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240
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Bryston
Ticks All The Boxes |
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It
has often been suggested to me that I should write reviews
of audio components from a repairer's perspective. The manufacturer's
commitment to on-going product support would also have to
feature in such reviews.
The problem would be though, an unvarnished appraisal of the
design, build quality, reliability and serviceability of many
products would probably get me into a lot of trouble!
In certain rare cases however, I would be prepared to make
an exception.
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And
this is a particularly rare case because unlike many of our
"regular patients" Bryston amps have a well-deserved
reputation for reliability and as such, are rarely seen in
the workshop.
When the owner of this14BST said that it made a LOT of smoke,
I assumed some exaggeration on his part -- until the lid was
removed to reveal what looked like scenes from Pripyat!
A large area of the power supply board was burnt and every
part was covered in soot.
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Two
large capacitors had obviously exploded and spewed electrolyte
all over the place.
The fibreglass circuit board was burnt right through where
heavy copper traces had apparently vaporised.
Heavy deposits of carbon and sooty debris were distributed
all through the unit along with a lot of goop from inside
the capacitors.
If this was going to be fixed, there would be a massive amout
of cleaning to do.
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So,
what happened? Underneath the circuit board, bridge rectifiers
supply the large capacitors which in turn, are supplied by
some fairly massive toroidal transformers.
It
looks like one of these rectifiers had shorted out and shunted
AC from the transformer. directly into the capacitors.
From the weight of the transformers, I would guess they're
good for about 1500 Watts, which is more than enough to bring
the capacitors to boiling point very quickly.
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The
bottom panel looked like a lunar landscape, heavily crusted
with debris. So, is this amplifier a write off - would you
even try to repair this? It would take hours just to clean
up all of the contaminated components before you could even
assess the extent of the damage.
Obviously the main power supply board is beyond repair so
it will come down to the manufacturer's commitment to support
legacy product. On the plus side, it is a Bryston and they
have a twenty year warranty, right?
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Well,
this one was a grey import so its warranty was void - but
- as it was (only) seventeen years old, they should still
have spare parts, right?
Right! Thanks to Bryston's support and the good folks at BusiSoft,
a complete power supply board, fully loaded with brand-new
parts arrived and was fitted into the freshly washed chassis
and tested prior to refitting the amp modules.
Someone at Bryston noticed a non-original part in the photo
that accompanied the spare parts request and decided to ship
replacement for that too - even though it hadn't been ordered!
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Now,
all the circuit boards have been thoroughly decontaminated
reassembled and tested and this amp is ready to go back to
work.
Apart from the cleaning which was a slow and messy business,
this amp is a pleasure to work on. It was obviously built
to last and also to be servicable.
Unlike many audio components that are constructed without
any considerations of servicability, this amplifier comes
apart and goes back together with precision like Lego bricks.
Everything aligns perfectly and the hardest part is figuring
out where to buy some of the weirdo Canadian screwdrivers
required.
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Conclusion:
Servicability is not just
about spare parts availability - it's also about free access
to technical documentation and a design that facilitates maintenance.
The 14BST puts a big tick in all three boxes and proves that
good design need not rely on exotic parts that will become
unavailable in a year or two. This means that not only will
it work for years, it will be be repairable for years in the
unlikely event that something does go badly wrong as it did
with this one. In terms of build quality and sonic performance,
it certainly ticks those boxes too.
So, if I was writing a review of this product and the company
that supports it, it would be a very positive one. At 600
Watts per channel, this is a very serious component and I
believe that anyone who owns such a beast has a right to expect
it to last. Surprisingly, very few supposedly high-end brands
would get a tick for all of the above aspects as many are
now utilising manufacturing techniques that rightly belong
in devices such as tablet computers and mobile phones and
therefore come with a similar use-by date.
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Reference
Re-Cap |
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These
mighty old monoblocks were in trouble. One of the gigantic
power supply capacitors had popped its cork. Electrolytic
capacitors contain electrolyte, a chemical which consists
mostly of water which, under normal conditions, should not
be pressurised - but if something goes wrong - either inside
the capacitor or outside of it, pressure can build up in the
can.
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In order to avoid explosions, large capacitors have a safety
valve to provide relief from pressure build-up. When a capacitor
loses enough fluid, it drys out and becomes defective. This
results in seriously reduced specification, an open circuit
or sometimes, even a short circuit.
The problem is that you can't get away with replacing just
the defective one... Why? Because when identical components
are subjected to identical conditions over time, they will
tend to have the same destiny - when one fails, you can bet
the others won't be too far behind.
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Also,
putting a fresh one in with a bunch of worn out ones is a
lot like putting one new tyre on your car while leaving three
bald ones on - not a particularly stable configuration!
The next problem is that nobody stocks these huge caps any
more - they either have to be custom made or bought as 'New,
Old Stock'... You might still get a set as factory spare parts,
ex- but you'll pay a truckload of cash for that.
We can however, make up the total C with smaller caps...
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Modern
super-amps don't use the big cans any more for a bunch of
reasons - but the main one is that a larger number of smaller
caps offers several advantages:-
They cost less, they're more compact, they cost less, they
perform better, they cost less, they're in production, they're
ex-stock - and did I mention that they're cheaper?
They perform better because smaller caps respond faster then
big ones do... (plus a whole bunch of other technical floobydust
that's beyond the scope of this particular blog).
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So...
four obsolete caps per monoblock - at 47,000uF are each replaced
with 5 x 10,000uF modern caps which, in addition to a slight
increase in capacitance, offer improved voltage and temperature
rating, lower source impedance and greatly improved response
time.
Unfortunately, we can't re-use those super funky brass bussbars
with the new array but some 1000 strand pure copper cable
does the trick nicely.
When we factor in the quantity discount on 40 x 10,000uF caps,
they end up costing less than two of the big capacitors -
assuming, of course, you could actually get the old ones!
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Conclusion:
These Gryphon Reference monoblocks
may be old but they are unequivocally awesome... the proverbial
iron fist in a velvet glove! Their story is not unique
however as there are many big amplifiers whose capacitors
are reaching their use-by date. As the giant capacitors
they used become unobtainable or prohibitively expensive,
we need to look to solutions based on obtainable parts.
Jobs like this are seldom completely straighforward as there's
calculation, planning and modification involved to accommodate
the different physical mountings and electrical connections.
The good news is that capacitor technology has come a long
way and smaller caps in parallel sound better than a single
large cap, as evidenced by the fact that all of the modern
super amps now use this approach. The total 400,000uF provided
by this array is more than adequate and in effect, provides
a power supply upgrade for the cost of a repair!
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A
citation for a Citation |
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ci·ta·tion [sahy-tey-shuhn]|
noun
Any
award or commendation, as for outstanding service, hard work,
or devotion to duty, especially a formal letter or statement
recounting a person's achievements.
Of all the upgrades I've done, few have been as satisfying
as this one... sure, it's just a little old 1970's amp but
well-loved and the results truly speak for themselves.
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I
refuse to do what I call the "idiot's upgrade" i.e.
just stuffing the box with fancy, expensive parts - instead,
I prefer to analyse the basic structure of the amp and improve
on that if possible.
Amps of this era were generally well made but there's a great
deal that's happened in amp design since.
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This
amp's owner decided that, after providing decades of enjoyment,
this baby deserved a major refurbishment. Following a few
discussions on options and possibilities, he decided to go
for 'the burger with the lot'...
See the numbered descriptions below for a summary of the actions
taken.
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1.
Mains input socket and wiring:
The original 'electric shaver cord' has been replaced with
an IEC receptacle which allows any high quality mains interconnect
to be used. The primary circuit wiring gets a makeover in
the process.
2.
On/Off Switch:
As the revised mains wiring requires only one primary
fuse, the remaining location is perfect for a suitably retro
on/off switch... why they didn't fit one in the first place?
Probably in anticipation of a switched outlet on the preamp.
3.
Three Way Binding Posts:
The original speaker terminals were not bad for an amp of
this era but were worn out and oxidised. The new gold binding
posts will take spades, bananas or open ends and fit the existing
chassis cut-outs perfectly.
4.
Gold RCA Sockets:
The original sockets were worn out and gnarly - you wouldn't
plug a decent interconnect into them even if it would fit.
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5.
Replace Main Filter Capacitors:
Modern caps are superior in every way to the originals which
are unlikely to meet spec anyway... In this case, one ot the
originals had been replaced by one which didn't match. As
we're rewiring these anyway, some new rectifiers go in too.
6.
Five Star Topology:
No, it's not a hotel room... This is our term for the
most musically correct method of wiring a single chassis,
twin mono amplifier. It's not about selling exotic wire...
it's about re-orienting current flows according to a design
philosophy and is by far, the single most significant aspect
of this modification.
7a,b.
Speaker Protection and De-thump Circuit:
The amp was capable of delivering a pretty good thump on power-down
and had primitive thermal breakers in series with the speakers...
while this did offer some protection, it was a sonic compromise.
A custom protection and de-thump circuit with high quality
speaker relays was fitted. |
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Conclusion:
This amplifier delivered
a real surprise by surpassing all expectations and to no small
extent. From first power-up after the rebuild, even dead cold,
it revealed undiscovered layers of information in a reference
recording that's been played many hundreds of times in this
place. For any component, at any price or quality level to
uncover something previously unheard in a very well-known
track is rare indeed.
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"The
time had finally arrived to find someone extremely capable
and trustworthy for the repair of my much loved power amp...
Im sure Dallas Clarke has been classified as a genius
with exceptional talent on countless occasions... "The
advice and craftsmanship he supplied for the repair and modifications
vastly improved the overall performance, exceeded my expectations
and were cost effective".
"Dallas Thank you ever so much for your incredible
work! The HK lives again, only to be cleaner, warmer and more
open sounding... and by the way, sometimes I can hear some
of those secret sounds in my music which I hadnt
experienced prior to your unique revamp.
Laurence S. Varrasso, Victoria Australia.
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Major
Rebuild: Bel Canto Orfeo |
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OK - this is a BIG one! A gorgeous old Bel Canto 845
SET had blown up badly - and then it sat for a while at the
local repair shop while the techs scratched their heads and
tried to guess what the heck it was!
First uh-oh! moment: Under the transformer cowling,
the power transformer had suffered a catastrophic melt-down.
(below, left).
Second uh-oh! moment: Urethane sealant, mixed with
carbon and debris from burnt insulation had flowed like hot
lava through the cable holes in the chassis (below, right).
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Third
uh-oh! moment, below: Under the chassis, the hot goop
had formed a lake on the PCB and set rock hard when it cooled.
There was no option but to remove all of it because it straddled
the 1200V supply. It took quite a while (using a heat
gun and a chisel) to remove the majority of the solidified
goop and debris which goes like toffee at about 100C.
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Below:
Stripped of components, the PCB was chemically decontaminated
and then reloaded with new components.
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After the top plate has been cleaned, a custom toroidal power
transformer is bolted into place. On the flip-side,
the repaired and upgraded circuit board is lowered into place
and connected for initial electrical stress-testing.
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Fourth
uh-oh! moment: The high-tension and heater circuits for
the big 845 valves are fine but both heater supplies for the
small valves are dead. The small yellow transformers that
supply this stage are burnt underneath... this points to power
surge as the prime suspect as it's the only explanation for
all of the transformer primarys burning out at once.
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Below:
A direct replacement is not available so a pair of (blue)
miniature sealed toroidal transformers are mounted in place
of the old yellow ones and then tied into the circuit with
some old-school point-to-point wiring.
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The
new heater circuits are soak-tested overnight before the amp
gets re-assembled and tested. Some minor adjustments
and the Bel Canto sings beautifully as its name implies.
Although this was a huge rebuild, its cost was still much
lower than a new one. Apart from that, the heartbreak
of throwing your favorite amp away doesn't bear thinking about!
Over the years I have been repairing, I have only written
off two valve units - and then only because their e-bay value
was less than the repair cost. This was one of the most
extensive repairs - but a good example of what can be resurrected
if you have the will..
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Fiat
Lux! - 38FD Valve Re-assignment |
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Unlike silicon chips, which go out of production soon as they're
no longer fashionable, valves never go out of date. Almost
all popular audio valves are still in full production and
readily available. Good news for lovers of valve amps!
But what about the exceptions -- the ones with rare and extinct
valves?
Are they destined for the scrapheap?
Classics like this gorgeous Luxman 38FD are in serious trouble...
their Compactron output valves have been out of production
for decades. The precious few that are left are rapidly running
out and are hideously expensive.
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By
the 60's, valve technology's dominance in comsumer products
such as black-and-white TV sets was slipping away fast. The
introduction of the Compactron series of valves was pretty
much an attempt to claw back some of this lost ground by offering
manufacturers smaller, more cost-effective valves for specific
applications.
If anything, Compactrons just made valves less attractive
by muddying the water... production didn't last as long as
the cheap TV sets they wound up in and the species went off
to join its friends, the Wooly Mammoth and the Yeti.
Few Hi-Fi manufacturers were seduced by the ill-fated Compactron
- unfortunately, Luxman was one of them.
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We've seen forum threads about modifying 38FDs to use available valves
but they balk at the prospect of changing transformers and the
limited choices in 12-pin valves.
But if the voltages and the sockets were taken out of the
equation, the 50CA10's electrical characteristics would not
be unlike those of a triode-connected 6L6 - which is one of
the commonest valves in the world... But then you'd have to
find some octal sockets that fit the chassis and then re-wire
the output stage and then somehow shoe-horn in an extra transformer
for the heaters...
Oh look... here's one we prepared earlier! |
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So,
now we're wired for mainstream valves, let's look at the selection
criteria... we need valves with dissipation similar to the
original Compactrons, smaller envelopes to fit in the tight
space, readily available, reasonably priced, reliable and
of course, premium audio valves.
These superb TungSol 5881s easily tick all those boxes and
are available in matched sets. They're a robust little performer
that just oozes quality and sounds lovely. The other ancient
Japanese valves get swapped with some nice new electro-harmonix
EF86's and 6AQ8s.
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After some testing, we replace a handful of components that
have gone off spec, re-fit the timber sleeve and apply a little
furniture polish.
The 38FD comes to life and it is immediately apparent that
it has regained all of its former glory and then some! After
years of gradual deterioration, it's easy to forget just how
good these old Luxmans used to sound... but this unit is now
wide awake and ready for work, surprisingly fresh and dynamic
but still with that legendary Luxman musicality.
Not all endangered valve amps can be modded for available
valves in this way, but this one's done and ready to make
beautiful music for the next 40 years!
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Defy
Logic |
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The
Jadis Defy 7 -- Impressive -- Heavy -- Lots of metal.
There are two ways to make good valve amps; you can either
draw upon the legacy of classic designs that have worked superbly
in countless products for many decades, perhaps even improving
on them (e.g. Conrad Johnson)...
- or a talented engineer could develop completely new and
patentable topologies that spawn a whole generation of new
audiophile products (e.g. Audio Research).
- or you could defy logic and make an amp like this one.
There's no nice way to say it... This thing has issues.
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The owner was a bit disturbed by the unit's failure. It made
an 'expensive smell' and then smoke came out.
Thirteen components showed either complete or incipient catastrophic
failure with several deep burns in the board. Further, it
was obvious that this was not the first time this unit had
failed in this manner.
Repair (i.e. just fixing what was broken) was therefore not
an option as there was obviously an underlying instability
which at first impression, seemed to be inherent in the design.
Further research would confirm this impression.
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A
little Googling turned up several accounts of Defy 7s blowing
valves, fuses and smoke. After the schematic was downloaded,
a comedy of errors unfolded. The driver stage was overrated
and overloaded, the output valves incorrectly biased. Below
every pentode, an incorrectly rated fuse failed to adequately
protect a badly designed cathode circuit. Almost every other
valve amp in the world uses a sacrificial resistor and/or
a B+ fuse. The fact that this amp has a dozen replacable fuses
in holders indicates awareness of a problem but not of its
cause.
Every part that's blown, fried or just wrong gets removed.
Carbon deposits are removed and the board gets patched.
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The old driver relied heavily on global feedback for linearity
and could scarcely control the Miller Effect of the pentodes
resulting in grid-positive runaways and red plating.
A new front-end and driver topology is selected and then optimised
by SPICE modeling software. The new topology (loosely based
on a Hafler/Keroes style phase splitter but employing dual
12AT7 SRPP gain/driver stages) is laid in point-to-point with
some teflon/silver links.
This provides plenty of clean, linear drive with buckets of
headroom and contol making it possible to correctly bias the
output stage for long-term stability and reliability.
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Twelve
sets of upgraded, corrected support components are installed
around the pentodes. Cleaned up, patched, re-loaded and re-configured,
the board is re-installed. A new heater elevation circuit
is added. Initial tests yield results consistent with SPICE
software modeling... a little tube rolling plus a tweak or
two and the unit comes up dead-centre, rock-solid.
Listen Test: Powerful and competant. Very much in control
of the load without losing valve amp detail and sweetness
- if anything, it has gained in this respect... Imaging, depth,
transparency - all in line with high-end expectations.
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Conclusion:
Above and beyond the scope of repair or upgrade, this job
amounts to a comprehensive design review. The question of
cost/benefit ratio arises. In this case, the unit was purchased
for a reasonable price and the work equated to approximately
30% of the purchase price. IMHO, the total outlay vs. the
end result represents a cost-effective solution. After six
months of flawless operation, the owner reports that it still
sounds stunning and very significantly better than it ever
did before the modifications.
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Servicing
The Gryphon |
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This amp quickly found a spot in my personal 'Top Ten'...
after it was fixed of course! An oldie, but a goodie, it's
still one of the largest, heaviest monsters around.
The DM-100 is rated at 100 Watts which is conservative to
the point of silliness, really. Despite the fact that it's
100% class A, this amp has seemingly bottomless reserves of
power and never seems to be working hard no matter what you
throw at it.
This
one had been serviced overseas and operated for a few months
and then mysteriously failed.
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There's
a triple decker sandwich of PCBs mounted to each of the large
heatsinks. You can't see the lower one (the current amp) in
this shot of the right rear corner, but you can see the voltage
amplifier PCB which has its own small heatsink and the voltage
amp's power supply which sits alongside the large white capacitors
on long brass legs.
This PCB had obviously been damaged due to improper re-assembly
when the amp was serviced overseas.
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The lower part of the the PCB had been badly deformed to the
extent that the components on it had been crushed up against
the small heatsink on the voltage board. The fact that it
operated for several months in this condition is a testimony
to the quality of this product.
It's very unusual to see a fibreglass PCB with such a huge
warp in it. The reason for the deformity does not become obvious
until the unit has been disassembled.
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After
lowering the big heatsink on the right side of the amp, the
reason for the deformity becomes clear... the corner of the
board has gotten snagged on a clinch-nut securing one of the
feet to the bottom panel (see magnified insert).
How on Earth did this amp go out in this condition? It's just
improper re-assembly, pure and simple - amazing it even worked,
let alone pass inspection!
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After the PCB is repaired and straightened, each of the blocks
(main power supply, current amplifiers, voltage amplifiers
and voltage supplies) are inspected, serviced, cleaned and
individually tested prior to re-assembly.
The
amp sections are then carefully lifted (as opposed to shoved!)
into
position, observing mechanical clearances.
As a final touch, the bussbars are removed and polished prior
to testing. After this amp has been on for an hour or two,
it's like a barby full of hot rocks but it sounds every bit
as good as you'd expect a big Gryphon to sound.
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Burmester's
Birthday |
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Another 'Top Ten' candidate, Burmester 911. This one had been
the centerpiece of a reference system for some time and had
convincingly wiped the floor with several high-end contenders
in A-B shoot-outs.
After many intensive listening sessions, a day came when this
911 lost its edge... it still worked - even sounded good but
that 'Je ne sais qua' was missing.
Difficult to discern what exactly was going on here - so let's
start with a general service and 'shampoo'.
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There
was no denying that the performance had dropped off - it wasn't
a massive change, but as it was enough to warrant investigation.
As this phenomenon was common to both channels, the logical
place to start was the power supply.
Close inspection of the underside of the PCB revealed signs
of mechanical stress in the soldered connections. After re-soldering,
the power supply is remounted and the rest of the amplifier
undergoes similar assessment.
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One thing that was very obvious about the Burmester, was its
ability to reveal subtle differences in interconnects and
power cables in any system it powered, so it's reasonable
to expect that this would extend to internal connections as
well. On inspection, some oxidation of internal connections
is noted, along with some loosening of crimp terminals.
Once all the connections had been cleaned and coated, re-tightened
and/or re-soldered, the amp is tested - and yes, it is once
again spine-tingling, as it should be.
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Audio
Research D-79 Restoration |
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Audio Research D-79 - I don't think there would be too many
audiophiles of my generation who haven't dreamt of owning
one of these at some point in time. Apart from being one of
the nicest amps to listen to, it looks like a very important
piece of equipment with those big groovy meters, knobs and
fuses.
The thing is though, there's just not that many of them in
the world - and if you've ever pulled one apart, you'll know
why - it has to be the most complicated valve amp ever made
and must have cost a fortune to manufacture.
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This
one was blowing fuses - lots of 'em and not just any old fuses,
the big ones that cost $15 ea!. The owner had only had it
a short time but it had clearly had a checkered history. The
first issue was that someone had tried to use the wrong fuses
and damaged the fuseholders so the front panel had to come
off to replace them. In the process, it became obvious that
this amp has been repeatedly fiddled with - repairs, 'upgrades'
and component substitutions were evident and really only making
things worse.
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The major issue however, came down to leaky capacitors...
the original capacitor bank consists of large can electrolytics
mounted on a PCB in a central compartment formed by two metal
partitions. There's just no point in trying to source replacements
for these... they would have been out of stock for maybe 30
years and the whole array only adds up to about 3,000 uF anyway.
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Translating
the capacitance and voltage requirements of this circuit into
current-production component values, we find that 28 modern
capacitors will do the job nicely. Of course, they're a different
size and shape so a new mounting arrangement has to be devised.
A special mounting bracket is fabricated to fix the capacitors
to the partition plate and the assembly is completed with
some old-school point-to-point wiring.
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The
new capacitor bank is fitted into the chassis. When finally
assembled, the other partition plate will help to keep fingers
away from the capacitors which will hold a lethal charge when
the unit is energised.
The new caps have slightly higher capacitance than the old
array and are superior, simply because of improvements in
the manufacturing process. While the amp is in this state,
several previous dodgy repairs are reworked in line with the
original standards of workmanship (looks like this amp's made
more comebacks than Rocky!).
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Underneath
the chassis, all the wires that attached the old capacitor
bank were carefully labeled so the final phase of re-assembly
is mostly about redressing the wiring looms to suit the revised
layout. When the wiring is finished, the unit is powered up
without valves to check the unloaded socket voltages. Valves
are then fitted and the unit is given a preliminary test,
alignment, burn-in period, realignment and finally a listen
test. Worth the effort to do it properly, this old classic
should sound lovely for years to come.
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Uh-Oh,
Chunder-Caps... |
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This is a nice little amp... it's a well balanced, competent
performer which drives most loads without a fuss and looks
the part as well. The Mark Levinson 331 has a comparatively
low resale value and can often be found online at a bargain
price. Team it with the right preamp and it will do the job
nicely in most systems.
So, what's the bad news?
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There's
a common issue with these, which appears to relate to a defective
batch of capacitors... which is possibly why they tend to
a bit 'bargain priced'.
Flip a 331 over (watch it, they're heavy and pointy!) and
you'll likely spot some dried-up, yellowish goop near one
or more of the round feet on the bottom panel.
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The culprit... one of four large blue capacitors in the power
supply. These components contain a chemical, composed mostly
of water, sealed inside the can. If, for any reason, they
overheat, pressure builds up inside the can until the relief
valve (the little round bit at about the 3 o'clock position
in the photo) pops and the cap disgraces itself all over the
joint. All four caps had dropped their bundle and it looked
like The Three Stooges had a pie fight in there!
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After
removing the big heatsink on the left side of the amp, we
can get access to the power supply for left channel. The two
smaller blue capacitors usually don't fail - the big ones
are the chunder-caps so the next task is to remove the clamps
and bussbars holding them in place.
Then comes the fun part - cleaning out the dried-up goop...
and then you get to do it all over again on the other side!
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After cleaning, we can replace the caps but the big blue ones
are very expensive and difficult to get... but why would you
want to put those back in there anyway?
This
array of smaller caps provides similar capacity, has a higher
thermal and voltage rating and their response time is faster
so they sound better. Oh, you want more? Sixteen of these
caps cost less than ONE of the big blue guys!
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The
finishing touch is to remove any traces of electrolyte spillage
from the baseplate. No rocket science here, just lots of hot,
soapy water and elbow-grease required.
This is a labor-intensive repair but the good news is that
what we save on parts nicely offsets the labor and you wind
up getting a sonic upgrade at no extra cost.
Overall, a worthwhile effort and a satisfactory end result.
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"Hi
Dallas,
Thank
you for your great work on my Levinson. It sounds very good,
even better than I expected. You are right, I probably had
not enjoyed its full potential for a long time, if ever, since
I bought it second hand."
Richard
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Phase
Ultra Linear |
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The legendary Phase Linear 700 Series II. Its performance
isn't exactly what you'd call 'State-of-the-art' but its bold,
gold panel and those oh-so-sexy Nightrider power meters have
undeniable appeal - and at 700 Watts, this baby still demands
attention. This
unit was in fine condition but had blown its outputs once
and then a second time after an inexpert repair attempt.
The choice: Should we jump through hoops to source
the obsolete parts required to restore it? - or - should we
give it a total makeover with some 21st. Century technology?
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Just
kidding... we already knew the answer to that one! The 700
wasn't the only super amp of its day but it was probably the
one that finally crushed the notion that valves would always
dominate in high wattage applications. This large array of
transistors is what delivers the grunt from that massive power
transformer. This unit blew a second time because the array
had not been properly repaired... it's not enough to replace
just 1 or 2 shorted transistors, the entire Right channel
cluster should've been replaced.
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The old output transistors were originally intended for use
in electric golf-buggies and were only used because they were
the biggest thing they could get their hands on back in the
'70s. Quasi-Complementary topology was dictated by the fact
that the transistors only came in one 'sex' but that's not
an issue these days, so the chassis gets rewired to accommodate
a Complementary-Symmetry array of super-matched audio transistors
which are heaps faster, tougher and more linear. The old gal
now has the output of a modern high-end amp!.
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After
modernising the output array, the drivers get an upgrade which
involves fitting some small flag heatsinks because the new
devices are a different physical shape to the originals. While
we're at it, the gain stage may as well get in on the makeover
so the old bootstrapped quasi-current mirror gets replaced
with a constant-current loaded Wilson configuration (seen
mounted on the custom heatsink across the rear) and the bootstrap
caps can now go straight into the trashcan. This faster, more
linear setup is more in keeping with the upgraded outputs
and drivers.
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Shakedown time. Prior to refitting the panels, the 700 gets
a major test and tweak session followed by a 48 hour burn-in...
and then it's time to rock the house!
These amps always reminded me of the muscle-cars of the same
era - heaps of straight-line grunt but no finesse but this
one has lost that 'industrial grunge' and deftly presents
a deep, wide soundstage with good spatial separation and dark
silences. Its resolution of fine detail is surprisingly eloquent...
but it still kicks like a crazy horse!
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"The
amp powered-up and in my system sounds stunning. Very quiet,
very detailed. Many thanks"
Bruce
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Ugly
Duckling Transformation |
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OK - I'll admit it - I looked at this and said: "No way!"
This
ugly little pile of scrap was supposed to be a Dynaco Stereo
120. Now, these were a popular kit and so there are a lot
of them around and sometimes the construction is a bit amateurish...
but this was not a pretty sight.
Plus, this one had been visited by the naughty technician
who had perpetrated some pretty dodgy modifications.
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There
wasn't any part of this amp that was unmolested - but the
owner was genuinely fond of it and was serious about bringing
it back to life so the job was on.
It was a bloody miracle this thing ever worked at all with
broken tracks, fried components and globs of solder everywhere
- eeeew!
The only thing for it was to strip it down to components,
assess what was reusable, replace what was not and then to
build a new Dynakit 120 from scratch.
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The PCB was littered with cuts and breaks and links and blobs
which were obviously someone's idea of upgrades but I couldn't
see any evidence that these changes were in any way improving
things.
After studying the original Dynaco manual, I decided that
the best course of action would be to restore the amp to original
spec and to do it right.
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I
mean... who on Earth has designed more amplifiers than David
Hafler? OK - this is some of his early solid-state work but...
who on Earth has designed more amplifiers than David Hafler?
I can't think of too many!
Rebuilt in accordance with the original design but using some
21st. Century semiconductors (plus a few tasteful tweaks and
some nice gold connectors), the Stereo 120 comes to life.
After a 48 hour burn-in period, this amp sounds fine - it's
a classic 60's sound that is very likable and about as good
as a result as could be expected from this chassis.
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"Dallas
Just thought I'd write to you to tell you how happy I am with
the Dyna re-build, you've done a great job! The amp was never
going to be a world beater but it sounds musical, smooth and
listenable. It sins are of omission, it doesn't add any harshness
etc. Anyway thanks again and next time I need any of my equipment
modded or repaired I'll call you."
Jon
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